On other ports (e.g. ESP32) they provide a complete Nimble implementation
(i.e. we don't need to use the code in extmod/nimble). This change
extracts out the bits that we don't need to use in other ports:
- malloc/free/realloc for Nimble memory.
- pendsv poll handler
- depowering the cywbt
Also cleans up the root pointer management.
STM32F0 has PCLK=48MHz and maximum ADC clock is 14MHz so use PCLK/4=12MHz
to stay within spec of the ADC peripheral. In pyb.ADC set common sampling
time to approx 4uS for internal and external sources. In machine.ADC
reduce sample time to approx 1uS for external source, leave internal at
maximum sampling time.
This commit adds the option to use HSE or MSI system clock, and LSE or LSI
RTC clock, on L4 MCUs.
Note that prior to this commit the default clocks on an L4 part were MSI
and LSE. The defaults are now MSI and LSI.
In mpconfigboard.h select the clock source via:
#define MICROPY_HW_RTC_USE_LSE (0) or (1)
#define MICROPY_HW_CLK_USE_HSE (0) or (1)
and the PLLSAI1 N,P,Q,R settings:
#define MICROPY_HW_CLK_PLLSAIN (12)
#define MICROPY_HW_CLK_PLLSAIP (RCC_PLLP_DIV7)
#define MICROPY_HW_CLK_PLLSAIQ (RCC_PLLQ_DIV2)
#define MICROPY_HW_CLK_PLLSAIR (RCC_PLLR_DIV2)
For use with F0 MCUs that don't have HSI48. Select the clock source
explicitly in mpconfigboard.h.
On the NUCLEO_F091RC board use HSE bypass when HSE is chosen because the
NUCLEO clock source is STLINK not a crystal.
Before this patch the UART baudrate on F0 MCUs was wrong because the
stm32lib SystemCoreClockUpdate sets SystemCoreClock to 8MHz instead of
48MHz if HSI48 is routed directly to SYSCLK.
The workaround is to use HSI48 -> PREDIV (/2) -> PLL (*2) -> SYSCLK.
Fixes issue #5049.
Enabled by default, but disabled when REPL is connected to the VCP (this is
the existing behaviour). Can be configured at run-time with, eg:
pyb.USB_VCP().init(flow=pyb.USB_VCP.RTS | pyb.USB_VCP.CTS)
The new fdcan.c file provides the low-level C interface to the FDCAN
peripheral, and pyb_can.c is updated to support both traditional CAN and
FDCAN, depending on the MCU being compiled for.
According to the schematic, the SDRAM part on this board is a
MT48LC4M32B2B5-6A, with "Row addressing 4K A[11:0]" (per datasheet). This
commit updates mpconfigboard.h from 13 to 12 to match.
- STM32F407VGT6 (1MB of Flash, 192+4 Kbytes of SRAM)
- 5V (via USB) or Li-Polymer Battery (3.7V) power input
- 2 x LEDs
- 2 x user switches
- 2 x mikroBUS sockets
- 2 x 1x26 mikromedia-compatible headers (52 pins)
https://www.mikroe.com/clicker-2-stm32f4
Mboot currently requires at least three LEDs to display each of the four
states. However, since there are only four possible states, the states can
be displayed via binary counting on only 2 LEDs (if only 2 are available).
The existing patterns are still used for 3 or 4 LEDs.
As per PEP 485, this function appeared in for Python 3.5. Configured via
MICROPY_PY_MATH_ISCLOSE which is disabled by default, but enabled for the
ports which already have MICROPY_PY_MATH_SPECIAL_FUNCTIONS enabled.
Before this patch I2C transactions using a hardware I2C peripheral on F0/F7
MCUs would not correctly generate the I2C restart condition, and instead
would generate a stop followed by a start. This is because the CR2 AUTOEND
bit was being set before CR2 START when the peripheral already had the I2C
bus from a previous transaction that did not generate a stop.
As a consequence all combined transactions, eg read-then-write for an I2C
memory transfer, generated a stop condition after the first transaction and
didn't generate a stop at the very end (but still released the bus). Some
I2C devices require a repeated start to function correctly.
This patch fixes this by making sure the CR2 AUTOEND bit is set after the
start condition and slave address have been fully transferred out.
Some SD/MMC breakout boards don't support 4-bit bus mode. This adds a new
macro MICROPY_HW_SDMMC_BUS_WIDTH that allows each board to define the width
of the SD/MMC bus interface used on that board, defaulting to 4 bits.
The previous version did not work on MCUs that only had USB device mode
(compared to OTG) because of the handling of NAK. And this previous
handling of NAK had a race condition where a new packet could come in
before USBD_HID_SetNAK was called (since USBD_HID_ReceivePacket clears NAK
as part of its operation). Furthermore, the double buffering of incoming
reports was not working, only one buffer could be used at a time.
This commit rewrites the HID interface code to have a single incoming
buffer, and only calls USBD_HID_ReceivePacket after the user has read the
incoming report (similar to how the VCP does its flow control). As such,
USBD_HID_SetNAK and USBD_HID_ClearNAK are no longer needed.
API functionality from the user's point of view should be unchanged with
this commit.
This new series of MCUs is similar to the L4 series with an additional
Cortex-M0 coprocessor. The firmware for the wireless stack must be managed
separately and MicroPython does not currently interface to it. Supported
features so far include: RTC, UART, USB, internal flash filesystem.
The new configurations MICROPY_HW_USB_MSC and MICROPY_HW_USB_HID can be
used by a board to enabled or disable MSC and/or HID. They are both
enabled by default.
In a non-thread build, using &_ram_end as the top-of-stack is no longer
correct because the stack is not always at the very top end of RAM. See
eg 04c7cdb668 and
3786592097. The correct value to use is
&_estack, which is the value stored in MP_STATE_THREAD(stack_top), and
using the same code for both thread and non-thread builds makes the code
cleaner.
stm32lib now provides system_stm32XXxx.c source files for all MCU variants,
which includes SystemInit and prescaler tables. Since these are quite
standard and don't need to be changed, switch to use them instead of custom
variants, making the start-up code cleaner.
The SystemInit code in stm32lib was checked and is equivalent to what is
removed from the stm32 port in this commit.
This is a start to make a more consistent machine.RTC class across ports.
The stm32 pyb.RTC class at least has the datetime() method which behaves
the same as esp8266 and esp32, and with this patch the ntptime.py script
now works with stm32.
If both FS and HS USB peripherals are enabled for a board then the active
one used for the REPL will now be auto-detected, by checking to see if both
the DP and DM lines are actively pulled low. By default the code falls
back to use MICROPY_HW_USB_MAIN_DEV if nothing can be detected.
When going out of memory-mapped mode to do a control transfer to the QSPI
flash, the MPU settings must be changed to forbid access to the memory
mapped region. And any ongoing transfer (eg memory mapped continuous read)
must be aborted.
The Cortex-M7 CPU will do speculative loads from any memory location that
is not explicitly forbidden. This includes the QSPI memory-mapped region
starting at 0x90000000 and with size 256MiB. Speculative loads to this
QSPI region may 1) interfere with the QSPI peripheral registers (eg the
address register) if the QSPI is not in memory-mapped mode; 2) attempt to
access data outside the configured size of the QSPI flash when it is in
memory-mapped mode. Both of these scenarios will lead to issues with the
QSPI peripheral (eg Cortex bus lock up in scenario 2).
To prevent such speculative loads from interfering with the peripheral the
MPU is configured in this commit to restrict access to the QSPI mapped
region: when not memory mapped the entire region is forbidden; when memory
mapped only accesses to the valid flash size are permitted.
Commit 9e68eec8ea introduced a regression
where the PID of the USB device would be 0xffff if the default value was
used. This commit fixes that by using a signed int type.
Entering a bootloader (ST system bootloader, or custom mboot) from software
by directly branching to it is not reliable, and the reliability of it
working can depend on the peripherals that were enabled by the application
code. It's also not possible to branch to a bootloader if the WDT is
enabled (unless the bootloader has specific provisions to feed the WDT).
This patch changes the way a bootloader is entered from software by first
doing a complete system reset, then branching to the desired bootloader
early on in the start-up process. The top two words of RAM (of the stack)
are reserved to store flags indicating that the bootloader should be
entered after a reset.
Previously the end of the heap was the start (lowest address) of the stack.
With the changes in this commit these addresses are now independent,
allowing a board to place the heap and stack in separate locations.
With this the user can select multiple logical units to expose over USB MSC
at once, eg: pyb.usb_mode('VCP+MSC', msc=(pyb.Flash(), pyb.SDCard())). The
default behaviour is the original behaviour of just one unit at a time.
Eventually these responses could be filled in by a function to make their
contents dynamic, depending on the attached logical units. But for now
they are fixed, and this patch fixes the MODE SENSE(6) responses so it is
the correct length with the correct header.
SCSI can support multiple logical units over the one interface (in this
case over USBD MSC) and here the MSC code is reworked to support this
feature. At this point only one LU is used and the behaviour is mostly
unchanged from before, except the INQUIRY result is different (it will
report "Flash" for both flash and SD card).
To use it a board should define MICROPY_PY_USSL=1 and MICROPY_SSL_MBEDTLS=1
at the Makefile level. With the provided configuration it adds about 64k
to the build.
It doesn't work to tie the polling of an underlying NIC driver (eg to check
the NIC for pending Ethernet frames) with its associated lwIP netif. This
is because most NICs are implemented with IRQs and don't need polling,
because there can be multiple lwIP netif's per NIC driver, and because it
restricts the use of the netif->state variable. Instead the NIC should
have its own specific way of processing incoming Ethernet frame.
This patch removes this generic NIC polling feature, and for the only
driver that uses it (Wiznet5k) replaces it with an explicit call to the
poll function (which could eventually be improved by using a proper
external interrupt).