Commit Graph

12 Commits

Author SHA1 Message Date
Brandon Satrom
48f67d007e feat: add Blues Swan R5 support
complete pin mapping for Feather pins

stubbed out files needed for complilation. still to be modified

0 out all CPY modules in mpconfigboard.mk until we get the build running

add csv for pin generation for STM32L4R5

add F4R5 references in peripherals files

refactored out board files BECAUSE I AM AN IDIOT; add L4 series system clocks file from CubeMX

took a guess at the number of USB endpoint pairs to get the build done

guess was close, but wrong. It is 8

clean up peripheral DEFs

Fixes build error:
```
In file included from ../../py/mpstate.h:33,
                 from ../../py/mpstate.c:27:
../../py/misc.h: In function 'vstr_str':
../../py/misc.h:196:1: sorry, unimplemented: Thumb-1 hard-float VFP ABI
 static inline char *vstr_str(vstr_t *vstr) {
 ^~~~~~
```
Sleuthing steps:
* verify that the feather_stm32f4_express board builds correctly
* put a `#error` at the bottom of the `mpstate.c` file.
* build for the feather and swan boards, with V=2 to capture the build command for that file.
* use a differencing tool to inspect the differences between the two invocations
* inspecting the differences, I saw a missing `-mcpu=cortex-m4` I tested by adding that to the Swan build command. The file built fine (stopping at the hard error, but no other warnings.)

A grep through the sources revealed where this flag was being set for the stm ports.

With this commit, the build gets further, but does not complete. The next exciting episode in this unfolding coding saga is just a commit away!

working build with minimal set of modules for the Blues Swan r5

chore:change header copyright name to Blues Wireless Contributors

USB operational.  Fixed up clocks to be hardwired for LSE no HSE case. (Trying to combine HSE in there made the code much more complex, and I don't have a board to test it out on.)

USART working

adds support for `ENABLE_3V3` and `DISCHARGE_3V3` pins.  I am surprised that pin definitions are quite low-level and don't include default direction and state, so the code currently has to initialize `ENABLE_3V3` pin as output.  The LED takes over a second to discharge, so I wonder if the board startup code is not having the desired affect.

short circuit implementation of backup memory for the STM32L4

all the ports

remove company name from board name to be consistent with the Arduino board definition.

add default pins for I2C, SPI and UART, so that `board.I2C` et al. works as expected.  Confirmed I2C timing.

fix board name

fix incorrect pin definition. add test to allow manual check of each output pin

analog IO

code changes for WebUSB. Doesn't appear to work, will revisit later.

ensure that `sys.platform` is available

checkin missing file

feat: make room for a larger filesystem so the sensor tutorial will fit on the device.

fix:(stm32l4r5zi.csv): merged AF0-7 and AF8-15 into single lines and removed extraneous headers mixed in with the data.

fix(parse_af_csv.py): pin index in the csv is 0 not 1, and AF index made 1 larger

chore(Swan R5): update peripherals pins from `parse_af_csv.py` output

optimize flash sector access
2021-09-28 18:52:02 -07:00
Jeff Epler
6ea136987e run codeformat 2021-08-19 13:54:13 -05:00
Jeff Epler
cabe96e188 canio: Run background tasks while waiting for message reception
Closes: #5004
2021-08-18 11:39:40 -05:00
microDev
a52eb88031
run code formatting script 2021-03-15 19:27:36 +05:30
Jeff Epler
16ed875f4e canio: remove unused fields
these relate to properties that were removed as well
2020-10-06 20:14:50 -05:00
Jeff Epler
81d7ef0256 stm: canio: remove stray optimization flag for debugging 2020-10-06 20:13:23 -05:00
Jeff Epler
eed3387f4e stm32: canio: Fix message cancellation
.. it's necessary to wait for a cancellation request to actually free
the respective Tx mailbox
2020-10-06 20:12:10 -05:00
Jeff Epler
abe0405d6e stm32: canio: Fix canio.CAN.restart() 2020-10-06 20:12:06 -05:00
Jeff Epler
e5a0af9216 stm32: canio: When Tx mailboxes are full, cancel an old message
.. also add the 8ms wait for transmission that the atmel sam port
has
2020-10-06 20:11:58 -05:00
Jeff Epler
a7dccb39a4 stm32: canio: remove unused functions 2020-10-06 20:11:51 -05:00
Jeff Epler
23bd2496de stm32: canio: remove some unneeded declarations 2020-10-06 20:11:43 -05:00
Jeff Epler
01e9e355ce canio: implement for stm32f405
The has successfully run my loopback self-test program for CAN,
which tests transmission, reception, and filtering.  The 1M baud rate setting
was also verified on saleae to be accurate.
2020-10-06 20:11:35 -05:00